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Re: Recent safety hazards at aging nuclear plants
Apologies to the list, but there follows a rather long response to Norms
posting which contains only a little reference to radiation safety (buried
in the eighth paragraph). Feel free to stop reading now if you wish
although I hope some of the following might be of general interest.
I am assuming (always a dangerous thing to do) that the author of the
article below is trying to indicate is that the age of the nuclear plants in
the US is leading to increasing safety problems which in turn have meant
more unreliable plant. In addition by referring to "the past three years"
he suggesting a worsening trend (Norm please correct me here if you think I
am wrong in my assumptions).
I have to say that I disagree both with the suggestion of increasing safety
problems AND that the trend is getting worse.
There are a number of key indicators (used both Nationally in the US and
Internationally) that can and are used to asses the performance of the US
nuclear plants, ALL of which have shown consistent long term improvement not
only for the last three years but in some cases as far back as 1980. These
include the following.
Unplanned capability loss factor - This is the percentage of maximum energy
generation that a plant is not capable of supplying to the electrical grid
because of unplanned shutdowns or outage extensions. A low value indicates
important plant and equipment is well maintained and reliably operated and
there are few outage extensions. This has gone from a value of 11.6% in
1980 to a low of 3.9% in 1998, 2.0% in 1999 and 1.7% in 2000.
Unplanned Automatic Scrams - the unplanned automatic scrams per 7000 hours
critical indicator tracks the median scram (automatic shutdown) rate for
approximately 1 year (7000 hrs) of operation. This has gone from 7.3 (per
7000 hrs critical) in 1980 to a value of 0.0 in 1998, 1999 and 2000. In
2000 59% of operating units had zero automatic scrams.
Safety System Performance - The safety system performance indicator monitors
the availability of three important standby safety systems to mitigate
off-normal events. For 2000 the goal was for > than 97% availability of
these three safety systems. In 1989 only 70% of the systems achieved the
2000 goal of > than 97% availability, In 1998, 98% of the systems achieved
this target and for 1999, 95% achieved this target and in 2000, 96% achieved
this target. Demonstrating that consistently high standards have been
achieved for the last three years.
In addition to those detailed above (which focus specifically on the safe
long term operation of the plants) Fuel reliability has increased year on
year from 1989 through to 2000. Chemistry performance (an important part of
ensuring long term condition of the plant) has been on an upward trend since
records commenced in 1994. Collective radiation exposures have reduced
dramatically since 1980. Median PWR collective doses for 2000 were
approximately 20% of those in 1980, median BWR collective doses were
approximately 17.5% of those in 1980. Volumes of Solid radioactive wastes
in 2000 were a fraction of those in 1980, 4% of 1980 values for PWRs and
7.5% for BWRs (m3 per unit - median value). Record highs (91.1%
approximately 3 times that used generally when assessing new wind projects
which are normally based an a unit capability factor of about 30%) in 2000
for unit capability factors. The lowest Industrial Safety Accident Rate
since 1980, 0.26 accidents per 200,000 worker-hours. All of the above
information was released by the Institute of Nuclear Power Operators (INPO)
and published in the May 2001 issue of Nuclear News (A publication of the
American Nuclear Society). All of the above indicates not a worsening trend
for the "ageing nuclear plants" BUT significant improvement year on year of
a number of key areas of plant operation.
Moving on I would like to review some of the incidents cited in the report
identified by Norm.
snip > January 1999: Inadequate maintenance led to a six-hour hydrogen fire
on the
roof of the control building at J.A. Fitzpatrick in Syracuse, N.Y., forcing
a plant shutdown.<snip
It is difficult to establish on the basis of the very brief summary the
seriousness of this incident. To my knowledge there are usually only two
areas on a nuclear plant where you might find Hydrogen gas (unless the site
has an electro-chlorination plant). One is as part of the purge system for
the reactor coolant treatment plant, used for chemistry purposes (oxygen
control in the reactor coolant minimising corrosion) and to remove
radioactive gases which are then treated in some way prior to discharge. I
am assuming that as no mention was made in the report of radioactivity, that
the fire was not related to this system as any vent would have been
discharging radioactivity and this would have been highlighted by the person
producing the report. the second area is in the turbine to cool the
turbo-generator. These systems do have vents to atmosphere but I would not
have expected them to have vented above the control building. However if
the fire did occur due to an excessive release of hydrogen from the
turbo-generator then this type of incident could have occurred at any type
of
large power generation plant. It is common to find fires on the non-nuclear
side of nuclear power plants reported while similar incidents at coal or gas
fired plants are not. While a fire on a nuclear plant should be treated
seriously, if it is confined to the non-nuclear areas it does not present a
significant danger to nuclear safety. As a final note of caution, even
though I feel I have a reasonable grasp of layout an construction of nuclear
power plants I am still only speculating. This illustrates how difficult it
is to assess this type of incident without much more information than was
given by the author of the original report!
snip > August 1999: A cooling- water drain line in Callaway, Mo., broke
because of severe corrosion, forcing a reactor shutdown. A subsequent
inspection revealed at least 10 areas where pipes had decayed and were in
danger of breaking.<snip
This type of statement is I believe intentionally misleading on the part of
the author. I have to admit to becoming particularly aggrieved whenever I
see the statement "cooling-water". I think it is used intentionally to
cause fear and alarm by those opposed to nuclear power. WHAT COOLING WATER
SYSTEM are we talking about. Off the top of my head I can come up with
many - component cooling water, essential service water, condenser cooling
water (often the one most talked about and having nothing to do with nuclear
safety), auxiliary service water, general service water, pond cooling water,
stator cooling water, cooling water to condition chemistry sample streams
etc. etc. etc. Faults with several of these cooling water systems could
have required the reactor to be shut down although none directly affect
nuclear safety. Again as no radioactivity was mentioned I am assuming that
the pond cooling water was not involved. If I was a betting man I would
place my money on either the component cooling water or on the main cooling
water system used to condense the steam after it has passed through the
turbine. In reality the intention of the original statement was to link in
the minds of the public the problem and the reactor. In general if you ask
a member of the public about the "cooling water" they assume it is the water
used to cool the reactor i.e. the Reactor Coolant System.
snip> 1999-2000: Millstone in Waterford, Conn., had to repeatedly shut down
due to
> > failures of the reactor control-rod drive system, including control rods
that came loose and dropped into the reactor. The plant operator blamed
failed insulation and damaged electrical leads.<snip
All this demonstrates to me is the inherent fail-to-safety characteristics
of
the design. Any loss of power to the control rod system results in the rods
entering into the core and prompting a reactor shutdown.
snip> February 2000: A steam generator tube ruptured at Indian Point 2 in
New York, contaminating 19,000 gallons of cooling water and releasing
radioactive steam into the atmosphere.<snip
This one is a difficult to regard as anything but an error on the part of
the operator and the NRC. While the consequences have been greatly
exaggerated, the SG which ruptured was, with the others at Indian point 2,
the last of that type in service. All SGs of that type installed at other
plants had been replaced. The owner had replacement SGs available and had
postponed the replacement of the installed SGs several times. In addition
there would appear to have been flaws in the SG inspection techniques and in
the approach adopted by the NRC to reviewing inspection results. The
overall outcome was an incident which has been advanced by Norm and the UCS
as an example of how both the industry and the regulator cannot be trusted.
snip > May 2000: A failed electrical conductor at Diablo Canyon 1 in San
Luis Obispo County triggered a fire that cut power to the coolant and
circulating water pumps that keep the nuclear core from overheating.<snip
Once again the lack of information makes it difficult to asses the real
potential for a significant incident. Jumping in with both feet again, I
find it difficult to accept that a single fire could result in the loss of
all reactor coolant pumps and circulating water pumps. Perhaps I am
demonstrating my ignorance but I did think that ever since the Browns Ferry
Fire important items of plant were placed on separate electrical supplies to
prevent just this type of incident. While it may be possible for a
significant fire to remove the primary supply to these pumps and cause them
to trip (although I didn't think that should have been possible) they should
definitely have been supplied by separate, independent supplies in the event
of a loss of primary supply. I suppose that a transitory loss of power will
however be advanced a loss of reactor cooling capability no matter how
transitory that may have been.
snip > August 2000: Peach Bottom Unit 3, in Pennsylvania, was forced into
emergency shutdown when an instrument valve failed and caused a leak of
contaminated reactor cool ant outside of primary containment. A similar
valve failure and leak of radiation had occurred May 28, 2000, but the
valves were not replaced.<snip
In order to asses this incident properly I believe the author should have
include the quantity of reactor coolant lost, the quantity of radioactive
material released and the actual rate of shutdown of the reactor. There is
no indication of a release to the environment, not that I would have
expected one in these circumstances. No indication of overexposure of any
workers. There is no information on the exact nature of the valve failure.
It is usual for the utility to undertake an investigation of this type of
incident when it occurs. Depending on the cause of the valve failure,
whether the problem lay with the maintenance or the installation or the
manufacture of the valve, I would have expected the operator to have
reviewed the operating, maintenance and installation history of that type of
valve on the plant, if the event was significant on other plants utilising
that type of valve and with the manufacturer of the valve. However if the
investigation did not identify the potential for a common failure mode,
either through incorrect installation, maintenance or manufacture then there
was little reason to remove other valves from service. Again while
highlighting the original problem the author of the report does not identify
what if any failures were responsible and where any deficiencies lay.
snip> October 2000: At V.C. Summer, in South Carolina, a 29- inch diameter
coolant pipe, with walls more than 2 inches thick, suffered a crack due to
water stress corrosion, creating a leak of radioactive cooling water. Crack
indications were later found at four more reactor inlets.>snip
Little comment to make on this incident other than it is a significant event
that is receiving significant attention from the operators and the
regulators.
snip > November 2000 to April 2001: After receiving a 20-year license
extension, operators of Oconee 1, in Seneca, S.C., found 19 cracks in the
reactor where control rods pass through to the nuclear core. Radioactive
cooling water had been leaking into the containment sump. In February nine
leaks were found in Oconee 3, which had been taken down for refuelling.
Oconee 2 was later found to have four leaking control-rod nozzles.<snip
I have already circulated my view on the generic issue of cracks around the
control rod drive penetrations. All I would add is that it is not clear
(although given that it was not stated it is unlikely) that the plant was
shut down prematurely. If this was identified during a routine shutdown (as
were the problems on Oconee 3) then any leakage must have been within the
operating constraints. It is not clear from the information presented here
and on the other related posting how these problems differ from long
standing issue with cracking of SG tubes.
Snip> January 2001: Failure of an 18-year-old valve at North Anna, Va.,
created a leak of radioactive coolant of more than 10 gallons per minute,
forcing a shutdown of the reactor.<snip
This incident appears to demonstrate the correct application of the
operating limits for the plant by the reactor operator. While the age of
the valve is included to add weight to the arguments about "ageing plant"
there is no information provided by the author to indicate that the age of
the component was responsible for the failure of the valve. Once again it
could have been a maintenance induced failure, a failure due to
incorrect/poor installation (defective welds etc.) poor plant chemistry
leading to excessive corrosion. If the author is trying to construct a
adequate argument to support his hypothesis on the age of the plant leading
to degraded safety he needs to provide more information.
snip > February 2001: A 20-year-old circuit breaker at San Onofre 3, near
Camp Pendleton, failed to close, creating a 4000-volt arc and fire that cut
power to coolant control systems, drowned emergency switching valves and
shut down emergency oil pumps, destroying the Unit 3 generator shaft.
Currently, 150 identical breakers remain in service at the plant.<snip
As with the previous incident there is no information provided which clearly
establishes
the age of the component as a contributory factor. Similar points exist for
the earlier
incident where two valves of the same design failed. There is nothing to
indicate that
there exists the potential for a common mode failure. The investigation of
the incident
should have addressed the potential for similar failures to occur and if no
action was
required to remove the "150 identical breakers" then without additional
evidence there
is no reason why these should not remain in service. Given that the major
item of plant
damaged by the incident was the Unit 3 generator it would indicate that the
fault occurred
on electrical systems associated with the non-nuclear side of the plant. As
such the "coolant
control system" referred to here were probably associated with non-nuclear
coolant systems
possibly the cooling water pumps used to condense the steam in the turbine
condenser. Quite
how the loss of emergency oil pumps should result in the destruction of the
generator shaft is
not clear. It is possible that the loss of the cooling pumps resulted in a
turbine trip. Following a
turbine trip the bearings for the turbine shaft would have required
additional oil to ensure that the
shaft did not come into contact with the white metal bearings.
snip > February 2001: After Arkansas 1 was re-licensed for 20 years,
extensive cracking was
found on the control-rod drives and thermocouple nozzles entering the
nuclear reactor.<snip
This definitely seems to be the issue of the month for anti-nuclear
activists. see previous comments
on this and the related posting.
snip > August 2001: Failure of a valve at Palo Verde 3, in Arizona, caused a
leak of radioactive
cooling water from the irradiated fuel-cooling pool into the reactor
containment building, forcing a reactor shutdown.<snip
Again there is very little detail provided by the author on the extent of
the leak neither the quantity of water
lost or amount of radioactivity released has been specified. We can assume
that there was no environmental
release, significant exposure to personnel, significant effect on the
cooling of the spent fuel pool or on plant within the containment building
(all of which would have been highlighted by the author).
To summarise, The author of this report can failed to produce a cohesive
argument to demonstrate that the safety of the US plant is decreasing and
more importantly in the light of the introductory statements, that the age
of the plants is at all relevant. With the exception of the cracking around
control rod drive penetrations, the report is simply a collection of random
events at nuclear plants that have been selected in an attempt to undermine
the confidence of members of the public in the safety of nuclear power. It
should be clear from the statistics provided by INPO that US power plants
have demonstrated consistent improvements in all key areas since records
were began and in particular that this trend has continued for the three
years referenced by the author of the original report.
Apologies for not having reviewed the original NRC reports of the incidents.
I would welcome comments from anyone who can provide more detail on any the
incidents cited above. It was unfortunately one of those occasions where I
think if I had tried to check the detail of each incident I would have
failed to respond to the posting at all. On this occasion I felt that
honest educated reasoning was preferable to a nil resposne.
Norm feel free to respond to any or all of the points I have raised.
Regards
Julian Ginniver
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